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Thread: Found fix for #7 piston problem

  1. #31
    Quote Originally Posted by ff_jeff View Post
    Naw the 9th piston gets bolted on to the block. Its independent. He only uses it for going in reverse. That way he doesnt blow hot exhaust fumes out the intake manifold.
    Looks like this
    That was good.
    99RCSB Broke because I wasted thousands and thousands of dollars on my truck.

  2. #32
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    Quote Originally Posted by LARRY01Z28 View Post
    I think allen is just joking.
    hes got to be,whos going to put one forged piston

  3. #33
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    Quote Originally Posted by LARRY01Z28 View Post
    I think allen is just joking.
    I know he's joking but I do believe that there are people not aware that this is a common issue. That was the reason for the explaination. I guess I forgot to put the REAL reason that #7 fails.......IT's THE TUNE!!

    2004 Silverado Crew Cab, forged iron 5.7, STS w/MP turbo, 10+ psi, FMIC, Tial 50mm BOV, Vic Jr, Snow performance meth, MTI Stealth cam .220/.220 .581/.581 115lsa, Comp chromoly pushrods, Yank TT3000 stall, LS1 Efans, 160 tstat, Trucool 40k trans cooler, 60# injectors, Walbro fuel pump, Patriot springs, Built 4l65E w/billet input & output shafts, Eaton posi, SD tuned...all installed by Klein North Automotive

  4. #34
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    I heard Allen's tunes break trannys. No one buy from him!




    jk.

    1969 Chevy RCLB C10 350/TH400 SOLD
    2007 Chevy RCSB 4.8 4x4 LS SOLD
    2008 Chevy RCSB 5.3 4x4 LT SOLD
    2010 Chevy CCSB 6.2 4x4 LT SOLD
    2005 GMC CCLB DRW 6.6 Duramax 4x4 191,000 and counting
    2013 FORD CCSB F350 6.7 Powerstroke 4x4


  5. #35
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    Quote Originally Posted by ramair2002 View Post
    This has happened in many different applications, FI, N20 & N/A, with different intakes, stock, LS6, Vic's... and fuel systems, return or returnless. The arguments are as follows:

    1) #7 is the farthest back and due to block design doesn't have adequate coolant circulation since there are block offs unlike earlier years that had cross overs.
    2) Returnless fuel systems can have trash build up in the fuel rails/injectors since there is not an inline filter and no way to return the trash to the tank.
    3) The stock intake design doesn't allow for even air distribution, especially in heavily modified applications, which cause #7 to run lean and not show on a wideband.


    These are the main arguments or theories. The problem is failure has occured when some of these are not present. For example, someone is running an aftermarket intake or upgraded fuel system and they still lose #7.
    Nothing has been absolutely, 100% proven to be the causing factor that I have read. IMO, I think that it's probably a combination of some of the above issues and not just one in particular. In addition, the factory clearances are set up tighter than what you would normally run in a highly modified set up which just adds another possibilty of reason for failure.

    If you have never heard of this being an issue, now you have!
    I heard of it just never knew what it was.
    "ALisSa1 Silverado"
    1990 Chevrolet RCSB 2002 Chevrolet Camaro LS1/4L60E
    Scrimpin Ain't Easy
    ( . Y . )


  6. #36
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    Quote Originally Posted by Chevy-Art View Post
    I heard of it just never knew what it was.
    I know!! That's the million dollar question!!!! The real reason for typing up that long post was for some of he newer people on the site who may not know the common problems and weak points when you start modifying. I wasn't directing it towards any one person.

    2004 Silverado Crew Cab, forged iron 5.7, STS w/MP turbo, 10+ psi, FMIC, Tial 50mm BOV, Vic Jr, Snow performance meth, MTI Stealth cam .220/.220 .581/.581 115lsa, Comp chromoly pushrods, Yank TT3000 stall, LS1 Efans, 160 tstat, Trucool 40k trans cooler, 60# injectors, Walbro fuel pump, Patriot springs, Built 4l65E w/billet input & output shafts, Eaton posi, SD tuned...all installed by Klein North Automotive

  7. #37
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    I didn't take it that way. I am glad to finally know what it is. Thanks Art...
    "ALisSa1 Silverado"
    1990 Chevrolet RCSB 2002 Chevrolet Camaro LS1/4L60E
    Scrimpin Ain't Easy
    ( . Y . )


  8. #38
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    I didn't know about the #7 piston failure til it happened to me but I do know my 02 sensors were bad, one side was dead and the other was really weak.

  9. #39
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    so in other words the design of the ls blocks are crap,cause 7 piston will always fail?well that sux if it cant be fixed

  10. #40
    ff_jeff Guest
    Quote Originally Posted by STUNNA View Post
    so in other words the design of the ls blocks are crap,cause 7 piston will always fail?well that sux if it cant be fixed
    wrx's have a similar problem with the #3 piston. These problems may not be completely cured, Having forged internals will eliminate most of the problem.
    I know the thought behind the Subaru piston failure was linked to the heat from the turbo. Maybe there is a similar situation with the LS motors. I know that the belief is less air flow. But maybe its extra heat, or a weakness to.

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