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Thread: WOW, just WOW.

  1. #1
    Join Date
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    WOW, just WOW.

    So a car is brought to me with a motor that was just rebuilt and has no oil pressure. Pull out the motor found the problem and put it back in. Perfect oil pressure, I let it idle for about 30 min to get all air out of coolant system and while i clean up the garage. Still perfect. Go for a test drive and it starts knocking REAL bad. Get back check rockers, all tight. Pull the motor yesterday and one rod cap is about halfway off. The rest are only finger tight.
    WOW, just WOW.
    Red 98 SUX2BU SS 11.04@121.69 with bolt ons RIP
    2003 White Diamond Escalade ESV AWD Long tubes, Comp cam 224/230 .581" .591" 114 lsa w/ dual springs, CAI, pulley, 05' E-fans, dual cut outs, Yank PT3200, Transgo shift kit, Billet 4th gear servo, Vette 2nd gear servo 8.976@77.16 MPH

  2. #2
    Join Date
    Apr 2005
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    TSP motor?
    Gone, but not forgotten!

  3. #3
    Join Date
    Oct 2005
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    drinking your alcohol
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    thats why people should use a checklist or a certain metod to do things like that instead of doing it all by memory...

    thats what we do when we build engines out here... it takes only 2 seconds to get distracted and forget that you only put them on hand tight instead of torqueing them down
    Quote Originally Posted by DamnYankee View Post
    lol...I wish you would never paint your truck...I bet it bugs them that much more that a primered up truck just soggied his Wheaties. good job buddy
    sprayedenali: i like catching, but not fishing
    DBTBSS: bring Tyler... we need someone to make fun of
    MidnightRider: your right im gay
    DamnYankee: my nana failed
    DamnYankee: confused...if it can't keep up to begin with, how can it keep up
    mitch cobb racing: ya, allen played with it for a while, HUGE difference

  4. #4
    Join Date
    Feb 2009
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    what was wrong with the motor?cause my motor was just rebuilt and did the same thing.how long did it take for you to fix it?cause my truck has been in the shop for three weeks now.hahaha. bad thing about it is the "mechanic"doesnt even want to answer my calls anymore

  5. #5
    MidnightRider Guest
    Quote Originally Posted by SCIV View Post
    TSP motor?
    +1 im definately going to LME after all the horror stories from tsp

  6. #6
    Join Date
    Jun 2008
    Location
    Houston
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    Quote Originally Posted by MidnightRider View Post
    +1 im definately going to LME after all the horror stories from tsp
    LME is allright but if ur goi g to drive all the way from houston might as well go to HKE and get an even better motor IMO
    74 Austin Morris Mini 1000 - Daily Coil Spring conversion, lowered, Disc Brake conversion
    FOR SALE: 04 RC/LB Duramax -12 second tow pig, built Allison, Tune, and supporting mods
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  7. #7
    Join Date
    Nov 2007
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    There are a couple of horror stories with HKE on this site. Maybe he'll chime in.
    Name: Mark,
    God created turbo lag so nitrous trucks could have a chance.


    http://www.ls1truck.com/forums/my-ga...tml#post274877

  8. #8
    Join Date
    Nov 2003
    Location
    Denton Texas
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    20,540
    My experience with them at first wasn't good but they made it right. They had a bad block, one of the main caps was sprung or something. They got another block and rebuilt the engine and all is good for two years now and 30+ bottles of spray.
    See my truck data in the "My Garage" section here... http://www.ls1truck.com/forums/my-ga...tml#post191709

  9. #9
    Join Date
    Jan 2008
    Posts
    8,031
    Sux 2 B U

  10. #10
    Join Date
    Apr 2009
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    Quote Originally Posted by gTeran1 View Post
    what was wrong with the motor?cause my motor was just rebuilt and did the same thing.how long did it take for you to fix it?cause my truck has been in the shop for three weeks now.hahaha. bad thing about it is the "mechanic"doesnt even want to answer my calls anymore
    Well the no oil pressure was due to a ripped oil pan gasket. All in all i've got maybe 10 hours into the car the first time and so far 4 hours this time with maybe 2 more to get it done. I work full time, go to school full time and am married full time so i can't just knock it out in one day.
    From another thread.
    Figured out what was wrong. The one on the right is what was in the car. The one on the left is an extra i had laying around.
    Last edited by SUX2BU; 05-19-2009 at 02:59 PM.
    Red 98 SUX2BU SS 11.04@121.69 with bolt ons RIP
    2003 White Diamond Escalade ESV AWD Long tubes, Comp cam 224/230 .581" .591" 114 lsa w/ dual springs, CAI, pulley, 05' E-fans, dual cut outs, Yank PT3200, Transgo shift kit, Billet 4th gear servo, Vette 2nd gear servo 8.976@77.16 MPH

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