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Thread: Tranny solved

  1. #11
    Join Date
    Jun 2008
    Location
    Ft worth tx
    Posts
    243
    He is a friend of mine, and he is not starving. Had four on the rack's and 2 holding for parts did me a favor and went ahead and pulled mine.

    Don't worry he isn't doing something for nothing I got his back!
    2004 Gmc VHO (LQ9), AEM cai, perma cool e-fans, aero turbine 3535,obx lt's,undedrive pulley w/overdrive alt pulley, lingenfelter 160 t-stat, zippy tune, taylor 10.4mm wires, tb bypass, Transgo HD-2 c, corvette servos, sonnax accumulator piston's,2600 stall,30,000 trans cooler lowered 1.5"/2", boss 313 22's on 285/45's, rollpan,shaved tailgate w/ss spoiler, painted interior, 2 solo l7 12's,custom fiberglass box,Pioneer F-900 Navi,SSS gauges,billet shiter and pedals,hid's (low's and fogs).

  2. #12
    Join Date
    Aug 2008
    Location
    North Texas
    Posts
    12,078


    My only sad feeling now is that I wasn't there when it broke so I could talk you into letting me fix it.


  3. #13
    Join Date
    Feb 2007
    Location
    Fort Worth
    Posts
    9,578
    Cool Ryan. Did he tell you any reason why the pump quit working?

    2000 ECSB 6.0L
    TORQUER V2 CAM ● COMP 918's ● 7.4 HARDENED PUSHRODS ● K&N SERIES 77 CAI ● 80mm BBK ●PACESETTER LT HEADERS AND 3'' ORY ● SUPER 40 FLOW ● 3000 STALL ● 4.10s ● BUILT 80e ● VORTEC PERFORMANCE TUNE ● MSD 8.5mm PLUG WIRES● ELEC. CUTOUT ● UD & ALT PULLEYS ● FLEX-A-LITE E-FANS ● 22" CENTERLINE STINGRAY III's ● LUND FIBERGLASS TONNEAU ● 2" LEVELING SHACKLES ● 12K HID LOWS & FOGS ● LEDs ● DEBADGED ● WHITE-FACED ESCALADE GAUGES ● KICKER 450.1 ● 2-CVR 10's ● DS60's ● K693's

  4. #14
    Join Date
    Jun 2008
    Location
    Ft worth tx
    Posts
    243
    He didn't have a clue, but the pump actually broke some peices inside it. I don't know enough about tranny's to really tell you what parts broke. But he said it was just it's time to go.

    He did tell me it was a redesigned pump cover, and there was one peice my shift kit wouldnt work with because of a new reverse boost valve, because the sleeve was shorter.
    Last edited by GMCvho; 06-05-2009 at 07:25 PM.
    2004 Gmc VHO (LQ9), AEM cai, perma cool e-fans, aero turbine 3535,obx lt's,undedrive pulley w/overdrive alt pulley, lingenfelter 160 t-stat, zippy tune, taylor 10.4mm wires, tb bypass, Transgo HD-2 c, corvette servos, sonnax accumulator piston's,2600 stall,30,000 trans cooler lowered 1.5"/2", boss 313 22's on 285/45's, rollpan,shaved tailgate w/ss spoiler, painted interior, 2 solo l7 12's,custom fiberglass box,Pioneer F-900 Navi,SSS gauges,billet shiter and pedals,hid's (low's and fogs).

  5. #15
    Join Date
    Aug 2008
    Location
    North Texas
    Posts
    12,078
    How long ago was the converter swapped and who did it. Bet it was 2K miles or less. The pump gear was shattered I bet.

  6. #16
    Join Date
    May 2008
    Location
    Schertz, Tx
    Posts
    2,539
    Dang Nathan...you sound like you're runnin' a shop out of your house (although I bet you could)
    I'm definitely gonna' remember you the next time we drive up to KS...

    07 Z71 4x4, 6.0L, 3.73s, Turbonetics T76 @ 10 psi, 75 shot, Snow meth kit, PLX DM-100 wideband gauge, Nelson tune, Comp 212/216 .557/.561 114 lsa, 60# injectors, Yank 3000, 4L80E , Magnaflow - dumped, e-cutout
    Line-X, Pace Edwards Full Metal Jackrabbit bedcover

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