Originally Posted by
zebra
okay... so here's a question for all y'all.
my truck: 99 NBS RCSB with a 4.3/5-speed & 4x4
at 135000, i switched from 10W-40 conventional to Mobil1 10W-30 & Wix filters. runs great for a year and a half... but now at 148400, i don't know all the specifics, but it has something to do with a bad rod bearing, a broken rod and the engine can now be best used as a boat anchor.
i was told by the mechanic (who is a long-time family friend & very trustworthy as well as having been mechanic-ing for 40yrs) that it was because i switched to full synthetic, & it washed off all the shellac on the bearings, which then collected in the bottom of the pan & clogged the oil pump. then he showed me at the very tip of the dipstick where it was a bit darker & thicker. that makes me wonder why i never heard of anyone else switching to synthetic & having the same problem.
have any of y'all ever heard of that scenario?